Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft

This project described the development of motorized shaft alignment system to be used in motor-pump machineries. Shaft alignment is vital to ensure the equipment able to operate for longer duration. It was well known that poor alignment causes the bearing failures, coupling wear or failure, increase...

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Main Author: Alkhanbashi, Maged Abdullah Ahmed
Format: Thesis
Language:English
English
Published: 2019
Subjects:
Online Access:http://eprints.utem.edu.my/id/eprint/25161/1/Improvement%20Of%20Self%20Alignment%20Footing%20System%20For%20Motor-Pump%20Rotating%20Shaft.pdf
http://eprints.utem.edu.my/id/eprint/25161/2/Improvement%20Of%20Self%20Alignment%20Footing%20System%20For%20Motor-Pump%20Rotating%20Shaft.pdf
http://eprints.utem.edu.my/id/eprint/25161/
https://plh.utem.edu.my/cgi-bin/koha/opac-detail.pl?biblionumber=117854
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spelling my.utem.eprints.251612021-09-29T11:34:04Z http://eprints.utem.edu.my/id/eprint/25161/ Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft Alkhanbashi, Maged Abdullah Ahmed T Technology (General) TJ Mechanical engineering and machinery This project described the development of motorized shaft alignment system to be used in motor-pump machineries. Shaft alignment is vital to ensure the equipment able to operate for longer duration. It was well known that poor alignment causes the bearing failures, coupling wear or failure, increase energy consumption, bearing housing damage and bent rotors or crankshafts. In the past, misalignment issues were solved manually by using shims, however, this method having problematic issue such as skill requirement and time consuming. Alternatively, the shimless footing system were introduced to overcome this problem. This project described the improvement of current shimless design by introducing motorized system. It was notified the root causes of the previous design problems due to manufacturing quality (t-slot and normal screw that used). A new motorize self-alignment system was developed along with fabricate a new footing system. A new feature will be added to overcome delay response time, backlash, not accurate positioning, and ease for maintenance. A linear bearing and backlash free screw are the major component to solve the backlash problem, reducing response time needed to settle down the misalignment correction, and become more precise. The new design of block was fabricated with size of 100 mm x 200 mm x 100 mm. The drawing of the prototype is done by using solidworks software. The block made of aluminum and machined by CNC milling machine. Vibration sensor was added to measure the response of misalignment. The PID controller will do correction by controlling shaft position by mean of step motor drive. Finally, the test on the fabricated system will be done by using test rig. As expected the project got improved in terms of response time with more accurate position. The lowest record score 7 seconds to correct the misalignment in shaft speed 100 RPM, while it took 86 second for correction in shaft speed 1000 RPM. 2019 Thesis NonPeerReviewed text en http://eprints.utem.edu.my/id/eprint/25161/1/Improvement%20Of%20Self%20Alignment%20Footing%20System%20For%20Motor-Pump%20Rotating%20Shaft.pdf text en http://eprints.utem.edu.my/id/eprint/25161/2/Improvement%20Of%20Self%20Alignment%20Footing%20System%20For%20Motor-Pump%20Rotating%20Shaft.pdf Alkhanbashi, Maged Abdullah Ahmed (2019) Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft. Masters thesis, Universiti Teknikal Malaysia Melaka. https://plh.utem.edu.my/cgi-bin/koha/opac-detail.pl?biblionumber=117854
institution Universiti Teknikal Malaysia Melaka
building UTEM Library
collection Institutional Repository
continent Asia
country Malaysia
content_provider Universiti Teknikal Malaysia Melaka
content_source UTEM Institutional Repository
url_provider http://eprints.utem.edu.my/
language English
English
topic T Technology (General)
TJ Mechanical engineering and machinery
spellingShingle T Technology (General)
TJ Mechanical engineering and machinery
Alkhanbashi, Maged Abdullah Ahmed
Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft
description This project described the development of motorized shaft alignment system to be used in motor-pump machineries. Shaft alignment is vital to ensure the equipment able to operate for longer duration. It was well known that poor alignment causes the bearing failures, coupling wear or failure, increase energy consumption, bearing housing damage and bent rotors or crankshafts. In the past, misalignment issues were solved manually by using shims, however, this method having problematic issue such as skill requirement and time consuming. Alternatively, the shimless footing system were introduced to overcome this problem. This project described the improvement of current shimless design by introducing motorized system. It was notified the root causes of the previous design problems due to manufacturing quality (t-slot and normal screw that used). A new motorize self-alignment system was developed along with fabricate a new footing system. A new feature will be added to overcome delay response time, backlash, not accurate positioning, and ease for maintenance. A linear bearing and backlash free screw are the major component to solve the backlash problem, reducing response time needed to settle down the misalignment correction, and become more precise. The new design of block was fabricated with size of 100 mm x 200 mm x 100 mm. The drawing of the prototype is done by using solidworks software. The block made of aluminum and machined by CNC milling machine. Vibration sensor was added to measure the response of misalignment. The PID controller will do correction by controlling shaft position by mean of step motor drive. Finally, the test on the fabricated system will be done by using test rig. As expected the project got improved in terms of response time with more accurate position. The lowest record score 7 seconds to correct the misalignment in shaft speed 100 RPM, while it took 86 second for correction in shaft speed 1000 RPM.
format Thesis
author Alkhanbashi, Maged Abdullah Ahmed
author_facet Alkhanbashi, Maged Abdullah Ahmed
author_sort Alkhanbashi, Maged Abdullah Ahmed
title Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft
title_short Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft
title_full Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft
title_fullStr Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft
title_full_unstemmed Improvement Of Self Alignment Footing System For Motor-Pump Rotating Shaft
title_sort improvement of self alignment footing system for motor-pump rotating shaft
publishDate 2019
url http://eprints.utem.edu.my/id/eprint/25161/1/Improvement%20Of%20Self%20Alignment%20Footing%20System%20For%20Motor-Pump%20Rotating%20Shaft.pdf
http://eprints.utem.edu.my/id/eprint/25161/2/Improvement%20Of%20Self%20Alignment%20Footing%20System%20For%20Motor-Pump%20Rotating%20Shaft.pdf
http://eprints.utem.edu.my/id/eprint/25161/
https://plh.utem.edu.my/cgi-bin/koha/opac-detail.pl?biblionumber=117854
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score 13.211869